Update nozzlewiper.cfg - Wait for servo move before turning off#1059
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eadz wants to merge 1 commit intoVoronDesign:mainfrom
Open
Update nozzlewiper.cfg - Wait for servo move before turning off#1059eadz wants to merge 1 commit intoVoronDesign:mainfrom
eadz wants to merge 1 commit intoVoronDesign:mainfrom
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The servo was turned off before it reached target angle.
Collaborator
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@chirpy2605 Any thoughts on this change? Given that it's your mod, does it look good to you? |
Collaborator
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Yeah, go for it. I've not had other reports of problems, but if it helps I see no problems adding it |
mjonuschat
approved these changes
Jun 22, 2025
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Hi, thank you for submitting your PR. Added/Changed mods detected in this PR:
Tool check results overview:
Tool check results details:SUCCESS: ✅File checker
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WARNING:
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| Item | Result | Reason |
|---|---|---|
| chirpy/NozzleWiper/images/NozzleWiper.gif | This file is larger than 2 MB! |
STL rotation checker
| Item | Result | Original orientation | Suggested orientation |
|---|---|---|---|
| Parallel_Arm.stl | ![]() |
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Fix for existing mod.
The servo was turned off before it reached target angle, which caused crashes. Simple fix.
my mod adheres to these rules.
license